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Thread: Motion madness - how to determine source of problem?

  1. #1
    Join Date
    Apr 2001
    Location
    South Elgin, IL
    Posts
    458

    Default Motion madness - how to determine source of problem?

    PRT 48x96 with 4G and PK296A1A SG7.2 motors

    I recently had one of my X motors start to fail and I had it rebuilt locally. I installed it and it works good - allowing me to finish a deadline job.

    On a different job a couple days later, the bot lost steps and cut through already cut sections and ruined the job.

    In using the keyboard or MX (any distance) the gantry shudders or shakes like it has Parkinsons. It's less noticeable when doing a Jog move but it's still there. There is some uniformity or regularity to the shakiness if that makes any sense.

    Thinking maybe a Gecko drive was causing it, I took the Y and Z Gecko drives and put them into the X drive locations on the board, and the X Geckos in the Y and Z locations. This didn't fix the problem so I ruled out the drivers.

    I checked my unit values, they're what I normally use.
    I tightened and loosened the turnbuckles but this made no difference.

    Now I'm wondering if one of the resistors near the Geckos might be bad or something else on the board - or the power supply? I don't know what the resistors should read...

    Could anyone having had similar problems give suggestions what to check next?

  2. #2
    Join Date
    Apr 2001
    Location
    South Elgin, IL
    Posts
    458

    Default

    OK in further testing, it's looking like turnbuckle tension may be the problem.
    When I make the X turnbuckles to the almost loose stage, the shuddering and the clattering noise disappears or becomes practically unnoticeable.
    Does this mean the turnbuckles are just magnifying an underlying problem, or are they causing the problem?

    I always ran the machine with the recommended number of turns on the turnbuckles and I always had clattering sounds like it was on a train track.
    But I thought that's just the way it is for these machines.

    At one time I thought maybe the X racks were not lined up to each other and I ran a string from the first X2 rack "groove" to the matching X1 rack groove. I then checked with a square against the rails and the string was square to the rails.

    I'm going to run another job now and see if everything is back to better than normal...

  3. #3
    Join Date
    Dec 2000
    Location
    Thorp, WI
    Posts
    2,845

    Default

    When is the last time you checked/replaced/greased the pinions?
    Scott




  4. #4
    Join Date
    Apr 2001
    Location
    South Elgin, IL
    Posts
    458

    Default

    Pinions were replaced in Feb. of 2015 and I cut EPS foam for about 90% of my work - which is only averaging 2-3 days a week at most.
    When I put the new pinions on, and greased the rack, there was no difference in the clackety clack sound I have always heard since day one.
    I'm now thinking either the recommended 4 turns of the turnbuckles is way too tight or that my motors have always had sloppy gear boxes.

    When the pinions are not engaged in the rack, or when I have the turnbuckles only tight enough to start moving the spring, there is no clacking sound when I move or jog in the X direction.

    When they are at the recommended tightness, one motor will make noise while moving in the positive X direction and the other motor will make noise when moving in the negative X direction. Never are both noisy at the same time.

  5. #5
    Join Date
    Apr 2007
    Location
    Marquette, MI
    Posts
    3,388

    Default

    Mayo...
    Mag a dial indicator onto the frame and set the point against the X car. Push pull to see how much, if any, play is in the system. Try both sides and check both variations of your spring tension to see if there is a difference. Also doesn't hurt to do the Y... on the motor side
    Gary Campbell
    GCnC Control
    GCnC411(at)gmail(dot)com
    Servo Controller Upgrades
    http://www.youtube.com/user/Islaww1


    "We can not solve our problems with the same level of thinking that created them"
    Albert Einstein


  6. #6
    Join Date
    Apr 2001
    Location
    South Elgin, IL
    Posts
    458

    Default

    I ran one small job with no problems. Today I started another small job and while cutting the 2nd piece, the X car once again jumped off the rails.
    I'm now thinking maybe something is running in the background that's interrupting the file and causing lost steps.
    I stopped the machine, opened task manager and did some screen captures of applications and processes.
    Will post those as soon as I transfer them to this computer.
    Gary - I will have to get a dial indicator - never used one before.

  7. #7
    Join Date
    Oct 2009
    Location
    Elgin Illinois
    Posts
    706

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    Mayo, you can borrow my dial indicator. It is an "A-Line-It Deluxe". But it does not have a magnetic base, which Gary said you will need. (Maybe I should have bought the "Ultra-Deluxe" model........ ) Chuck
    Chuck Keysor (circa 1956)
    PRT Alpha 60" x 144" (circa 2004)
    Columbo 5HP spindle
    Aspire 9.0, Rhino 5

  8. #8
    Join Date
    Apr 2001
    Location
    South Elgin, IL
    Posts
    458

    Default

    This morning I made changes based on the Black Viper "tweaked" settings for the Windows 7 Pro Service pack 1.
    Initial results seem that the computer is faster responding.
    I ran one job of 20 pieces and so far so good. Maybe I shut off whatever was interrupting the bot... time will tell.

  9. #9
    Join Date
    Apr 2001
    Location
    South Elgin, IL
    Posts
    458

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    Continuing to have problems with motors not acting as they should... updated info -
    When I first got my 4g board, I was able to jog at 6 inches per second.
    After dealing with steps or ridges in cuts I decided to lower the jog speed to 5. This worked for some time and the missed steps seemed to be happening less frequently. It didn't eliminate the ridges completely though.

    Yesterday the motors missing steps started happening again for no obvious reason.
    So I dropped the X motors away from the rack and when I did a jog move the motor(s) would make a higher pitched sound after about 24 inches of travel, based on the numerical readout since they weren't actually moving the gantry. I then experimented with changing the jog speed and found a speed of 4.99 did not stall the motors but 5.0 does stall them or make them out of sync. The sound of the motors after traveling approx. 20 to 24 inches in X distinctly changes to a higher pitch and then looses steps when my jog speed is 5 or higher.

    Incidentally, when I ran the speed test program, the result was over 73%.


    Why would a jog speed of 6 have worked for some time but now I'm only able to jog at 4.99 ?
    Has some other setting been changed inadvertently that I'm not aware of?
    The only thing I changed (today) was making the slow corner speed from 60 down to 50.
    I don't even know what else to check at this point.

  10. #10
    Join Date
    Mar 2004
    Location
    Delray Beach, FL
    Posts
    3,708

    Default

    pinions, proper tension on motor springs, grease on rack, tightness of gantry bolts and squareness of gantry.

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